Analisis Kinerja Simpang Tak Bersinyal Menggunakan Metode Pedoman Kapasitas Jalan Idonesia (PKJI 2023). (Studi Kasus: Jalan Pramuka Dan Jalan Sembilang Kota Pekanbaru)

Najiha, Siti (2024) Analisis Kinerja Simpang Tak Bersinyal Menggunakan Metode Pedoman Kapasitas Jalan Idonesia (PKJI 2023). (Studi Kasus: Jalan Pramuka Dan Jalan Sembilang Kota Pekanbaru). Undergraduate thesis, Politeknik Negeri Bengkalis.

[img] Text (Abstract)
1. SKRIPSI - 4204201287 - ABSTRACT.pdf - Submitted Version
Available under License Creative Commons Attribution Share Alike.

Download (184kB)
[img] Text (BAB I PENDAHULUAN)
2. SKRIPSI - 4204201287 - BAB I PENDAHULUAN.pdf - Submitted Version
Available under License Creative Commons Attribution Share Alike.

Download (412kB)
[img] Text (Daftar Pustaka)
3. SKRIPSI - 4204201287 - DAFTAR PUSTAKA.pdf - Submitted Version
Available under License Creative Commons Attribution Share Alike.

Download (288kB)
[img] Text (Full Text)
4. SKRIPSI - 4204201287 - FULL TEXT.pdf - Submitted Version
Available under License Creative Commons Attribution Non-commercial Share Alike.

Download (3MB)

Abstract

The intersection of Pramuka Street and Sembilang Street is a meeting point of provincial roads leading to Pekanbaru City and other cities on major roads, while on minor roads are roads leading to Siak Regency and Bengkalis Regency so that on weekdays and holidays at certain hours there are often delays and queues of vehicles because the traffic flow is quite busy. Therefore, a study was conducted to determine the level of service and how to improve the performance of unsignalized intersections. This study uses the Indonesian Road Capacity Guidelines (PKJI 2023) method as a reference in the study. The results of the intersection analysis showed that the highest traffic volume occurred in the research results on Monday, February 19, 2023, at 07.00-08.00 with 2.414.8 pcu/hour; degree of saturation 0.75 with a capacity of 2.414.8 pcu/hour, intersection delay (T) of 17.85 sec/pcu, and the queue opportunity value (PA) ranged from 23% - 46%. After the alternative, namely eliminating the right turn direction in existing conditions, the capacity (C) increased to 3207.447 pcu/hour. The degree of saturation (DJ) value decreased by 0.50 with a capacity of 1.595 smp/hour, intersection delay (T) of 11.38 sec/smp and queue opportunity (PA) ranging from 11%-25% for the road performance index to increase to B. Keywords: Traffic Flow, Unsignalized Intersection Performance.

Item Type: Thesis (Undergraduate)
Contributors:
ContributionContributorsEmailNIDN/NIDK
Thesis advisorLisya, Mutiamutialisyaa@gmail.comNIDN1005069601
Uncontrolled Keywords: Keywords: Traffic Flow, Unsignalized Intersection Performance.
Subjects: 410 ILMU TEKNIK > 420 TEKNIK SIPIL DAN PERENCANAAN TATA RUANG > 421 Teknik Sipil
Divisions: Jurusan Teknik Sipil > Sarjana Terapan Teknik Perancangan Jalan Dan Jambatan > TUGAS AKHIR
Depositing User: D4 TPJJ A 2024
Date Deposited: 24 Aug 2024 04:05
Last Modified: 24 Aug 2024 04:05
URI: http://eprints.polbeng.ac.id/id/eprint/13583

Actions (login required)

View Item View Item